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Oulton Park 16th Feb 2018

Took the bike to Oulton for a very cold trackday. Mate wanted to have a ride on his donor bike 640 supermoto. Thought It would be good for a comparison. Top temp for the day was about 7-8 deg C
He is a bit braver (younger) than me, but I managed to keep up. even made a couple of passes. I think I have the edge on power and the handling is much better with the new shock, it on rails now. I can tip in exactly where I want to be and it holds a line perfectly, very stable and I didn't have a moment all day. They had to put salt down on Shell oils hairpin and delayed the start of the day for an hour
to let the ice melt. A few of the faster groups had crashes braking for the chicane after shell oils and that may have been ice still in the track surface. By the time we went out it was a bit better but we still took it steady. After lunch we swapped bikes for one session but I didn't go very well on the supermoto, its just too comfortable, felt like I was out for a cruise. I need to do another strip down on the rear end as I think there is too much vibration and I suspect the back engine mount may have some play. The swing arm shaft goes through top hat spacers in the back of the engine case and I think that I might need to make some new top hat spacers. Carb I think needs re jetting so ill do that too. Otherwise I am very pleased.

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Engine Vibrations

Well after riding Stuarts 640 supermoto and this bike back to back, the vibration had to be coming from somewhere. The rear mount was one thing I hadn't paid too uch attention to when I started the project. Stripped it down at the weekend. I dropped the back of the engine and managed to drift one of the top hat spacers out, but the other one wasn't  having it. Decided to take engine right out to get better access. Was thinking I might have to drill it out. Made a drift from a long stainless bolt and machined the head in the lathe making the lip thinner eventually, with the lip about .5mm thick I got a good contact with the end of the bush and got the bugger out. Both the spacers were about 1mm oversize on the ID so the back of the engine had about 1mm of play.  Next job is to make some new spacers and fit them, have ordered some bar stock for that. May move the oil cooler while its apart.

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